Went to the club and ran the GP60 on September 16. The biggest problem I had was loading and unloading the locomotive. This loco is big and very heavy compared to the little steamer I have, so I will have to build a steel rack to hold it in the back of my truck.
Arrived at the track at 5:30 PM and unloaded. Boy! That was almost as much fun as the 2 hours it took to load at my house. Anyways, got it out on the track and topped all the fuel and oils off, took the body off and fired it up.
First thing that was incorrect was the control arm/handle. It was hitting the riding car when reversing and the draft gear couplers were moved too much. I will make a new handle and put in a draw bar to couple the engineer car to the locomotive.
On the main line it ran well so I put my son Wyatt on it to run it around. This allowed me to stand back and see and hear how it was running. I adjusted the carb and it smoothed right out. About that time Rory Hawkins arrived after he had finished his day job. Rory got on the train and gave it a run. I then played with the detent adjustment on the splitter valve with Rory moving it to get it set so that it had a good feel. We then ran it around the track a few more times.

The unit seemed to smoke some and had a "pop pop" sound from the exhausts. Funny thing is I told Rory that I had put some ring sealing oil in it so it should fix itself. We put Wyatt back on it and let him just run the heck out of it when I herd the exhaust sound had changed. It got very quiet and the unit started to smoke a little more. I thought "oh no" now here comes some work. We got Wyatt to stop, and I could feel the body sides were hot, so I pulled the body off and Rory found out that it had blown off the small muffler that I had put in just before the dump out pipe on the exhaust and the paint on the muffler rapper was burning off a little. After it sat there running for a few minutes it stopped smoking and it was running very quietly: Hmmm, like I said it fixed itself. Wow, sometimes I scare myself.
We then headed off down the Crenshaw Line when the cable on the throttle slipped so I adjusted it back. About half way down the line I got behind the controls and opened her up. It is just one of these "race car things" I learned years ago on how to test a new unit, and man, this thing can really get going. I was very surprised how fast it would go. It fits on the 1/2 turn table with 6" to spare as it has a long riding car on it for a three-man crew which makes the whole unit longer than most.
I had to readjust the cable again then Rory ran it back in the dark as I blew out the headlight when making adjustments to the throttle. As we were running along, the unit got very quiet. Rory said the cable had slipped again, but it was still just running along. Man! It was so quiet and with no head light, the people on the walking path didn't know we were there just a few feet away.
Well, I would say it was a good test run, with only a few things to change and yes, it took way too long to load it back in my truck. Good thing Rory was there too help. So now it's off to the Orange County Fall Meet and I'm thinking it will do just fine.
The funny thing is, all this felt just like getting one of my new race cars on its first run something I learned from my dad and now have passed on to my son, Wyatt. To see how you can build or rebuild something from just a pile of parts and odds and ends. Man! it feels so good to have a successful run after changing so many parts of this unit. Tom D.
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